Rebuilt and going strong!!!
Posted: 19 Aug 2008, 11:29
Hi again,
Just finished the rebuild on my mark 2,
the wossner oversize piston went straight in (as it should), thankfully i checked th rc valve before sealing it all up as it was going to foul on the piston, which i'm sure would not be pretty!!
Anyway, i filed it down and reassembled the motor, changed the oil and added fresh coolant.
Second kick it fired up and idled straight away!!
After putting around for a couple of hours, i decided to open the throttle in first and needless to say, i was quite impressed. the front wheel became airborne quite easily.
I did disconnect the oil pump and am now premixing the fuel at 40:1, i'm pretty sure the pump is what caused the first seizure.
I also grabbed a new sticker kit to tidy it up a bit, looks a treat now.
Looking forward to some really good rides now, starting with a big one this weekend, hopefuly all goes well!
Just finished the rebuild on my mark 2,
the wossner oversize piston went straight in (as it should), thankfully i checked th rc valve before sealing it all up as it was going to foul on the piston, which i'm sure would not be pretty!!
Anyway, i filed it down and reassembled the motor, changed the oil and added fresh coolant.
Second kick it fired up and idled straight away!!
After putting around for a couple of hours, i decided to open the throttle in first and needless to say, i was quite impressed. the front wheel became airborne quite easily.
I did disconnect the oil pump and am now premixing the fuel at 40:1, i'm pretty sure the pump is what caused the first seizure.
I also grabbed a new sticker kit to tidy it up a bit, looks a treat now.
Looking forward to some really good rides now, starting with a big one this weekend, hopefuly all goes well!