MK1 Piston seizure
Posted: 31 Aug 2009, 14:18
Heading up to Eastleigh on Sat morning to go on a trail ride with the local TRF. I took the motorway as I was running a wee bit late and it was only about 10 miles. Doing a steady 70mph and the engine cut, no warning, just died like the kill switch had been hit. Briefly twisted the throttle a wee bit but no effect so then disengaged the clutch and coasted to the side. Doing about maybe 20mph on the emergency lane and dump the clutch again just to see if it'll catch and the back wheel locks this time. Come to a stop, get off, remove me helmet and Camelback and try kicking it. the engine is free now but I can turn it with my hand, no resistance.
Missus comes to collect me in the Tranny and get it back home and remove the head expecting to see a big hole in the piston, but instead this is what I see.
http://i14.photobucket.com/albums/a340/ ... C02906.jpg
http://i14.photobucket.com/albums/a340/ ... C02909.jpg
I'm not great with s strokes but thought the plug looked OK ish
http://i14.photobucket.com/albums/a340/ ... C02914.jpg
I rebuilt the bottom end a few months back and it's been out on the trails half a dozen times since with no dramas. I usually van it to the trails and then back home again as it's often around an hours ride to the start of Salisbury Plain or up Basingstoke way which is where I normally ride. I've had it up to 70 a coupla times on brief bursts and it's felt fine.
Since I rebuilt it, it's felt very hesitant about midrange when giving it a handful. Felt like a four firing on three, so had to drop a gear or two then rev it through that patch and then it's extremely willing.
I had a feeling this was an over rich mixture and as when I got it a coupla months ago the needle was set on the second from top groove (one weaker than the centre of the five grooves) I decided to put it there again after dropping the carb in the ultrasonic tank to give it a good clean.
Set of with the new needle setting and it felt much better, barely a hint of the previous hestitancy.
It felt willing on the motorway just prior to the seizure, not stressed and plenty left in hand, but I was happy at 70 and didn't want to overdo it.
1 So what do you think happened?
2 Why did it cut out?
3 Why did it not seize immediately when it cut out?
4 Why did it seize shortly afterwards?
5 Why no compression?
6 It's on +1.50, do I have enough for another rebore?
7 How much is a new piston and rebore?
8 Anybody want a MK1 with a small fortune in receipts once I've rebuilt it? (again)
cheers
Millard
Missus comes to collect me in the Tranny and get it back home and remove the head expecting to see a big hole in the piston, but instead this is what I see.
http://i14.photobucket.com/albums/a340/ ... C02906.jpg
http://i14.photobucket.com/albums/a340/ ... C02909.jpg
I'm not great with s strokes but thought the plug looked OK ish
http://i14.photobucket.com/albums/a340/ ... C02914.jpg
I rebuilt the bottom end a few months back and it's been out on the trails half a dozen times since with no dramas. I usually van it to the trails and then back home again as it's often around an hours ride to the start of Salisbury Plain or up Basingstoke way which is where I normally ride. I've had it up to 70 a coupla times on brief bursts and it's felt fine.
Since I rebuilt it, it's felt very hesitant about midrange when giving it a handful. Felt like a four firing on three, so had to drop a gear or two then rev it through that patch and then it's extremely willing.
I had a feeling this was an over rich mixture and as when I got it a coupla months ago the needle was set on the second from top groove (one weaker than the centre of the five grooves) I decided to put it there again after dropping the carb in the ultrasonic tank to give it a good clean.
Set of with the new needle setting and it felt much better, barely a hint of the previous hestitancy.
It felt willing on the motorway just prior to the seizure, not stressed and plenty left in hand, but I was happy at 70 and didn't want to overdo it.
1 So what do you think happened?
2 Why did it cut out?
3 Why did it not seize immediately when it cut out?
4 Why did it seize shortly afterwards?
5 Why no compression?
6 It's on +1.50, do I have enough for another rebore?
7 How much is a new piston and rebore?
8 Anybody want a MK1 with a small fortune in receipts once I've rebuilt it? (again)
cheers
Millard