AR missing / 4 stroking at low revs
AR missing / 4 stroking at low revs
Help!! Only had the bike about a week and noticed that occasionally the bike runs very erratically at low revs. Not like that all the time. I've had the carb off, cleaned it out and jets blown through with compressed air. Checked the exhaust valve and it seems to move freely. Ran bike with AR cover off and valve moves when revs rise. Starting to suspect electrical fault but all symptoms are like a fuelling problem. Anyone had same problem?
- mickstoy
- Regular Visitor
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- Posts: 178
- Joined: 27 Oct 2006, 13:07
- Location: biddulph stoke on trent
as jon says it does sound like jetting is the bike running standard and is it still running standard jets? have another look at the holes in the jets if the bikes been stood for a while with the carb full of fuel it will go staleand leave a crud coating on everything, commpressed air may not be enough to clean it. try poking a nylon bristle through the jet and maybe fire some carb cleaner through it the holes are tiny and dont need much to affect them. when i bought mine it had been stood for about twelve months and it took four attempts on the carb to sort it out (it was running similar to yours!)
good luck
good luck
91 mk2
Removed carb. Found tiny pieces of black debris in bottom of float bowl which suprised me as I'd only just had the carb off a few days before. Pilot jet and main jet removed and blown out. Nylon bristle pushed through all clear. New fuel pipe and inline filter fit. Bike rebuilt. Took it for a test ride...... you guessed it no better. In fact if anything it seems worse! Gonna ring Leisure Trail and get a new pilot jet. Anyone any ideas?
[b]knobby :[/b]
> Removed carb. Found tiny pieces of black debris in bottom of float bowl which
> suprised me as I'd only just had the carb off a few days before. Pilot jet
> and main jet removed and blown out. Nylon bristle pushed through all clear.
> New fuel pipe and inline filter fit. Bike rebuilt. Took it for a test ride.
> ..... you guessed it no better. In fact if anything it seems worse! Gonna ring
> Leisure Trail and get a new pilot jet. Anyone any ideas?
Have you tried flushing out the petrol tank
Maybe sh** in the tank could be blocking the jet's and the fuel filter 
> Removed carb. Found tiny pieces of black debris in bottom of float bowl which
> suprised me as I'd only just had the carb off a few days before. Pilot jet
> and main jet removed and blown out. Nylon bristle pushed through all clear.
> New fuel pipe and inline filter fit. Bike rebuilt. Took it for a test ride.
> ..... you guessed it no better. In fact if anything it seems worse! Gonna ring
> Leisure Trail and get a new pilot jet. Anyone any ideas?
Have you tried flushing out the petrol tank


Mud, Sweat and Fear
91-MK2
91-MK2
Thanks Gwyn. Very little dirt / muck in the fuel filter. Think the black bits were coming from the float bowl seal. Someone had put sealant on there! Cleaned it off now. Rang LT and ordered the pilot jet. Chap I talked to suggested changing supressor cap. Just done that, seemed better at first but within a few miles same missing / stuttering fault appeared. Does seem to be at small throttle openings. Will wait now for the pilot jet to arrive unless someone comes up with something else to try.
Think we've sorted it! Put a new O ring on the air screw, had a test run but no difference. Put in the new pilot jet and went out again. Bike better but still sputtering at low revs. Air screw was set correctly at 1 and a quarter turns out so came out another half turn. Instant improvement. Out another quarter of a turn and I think I'll leave it that!! Best I've had it running. Thanks everyone. Special thanks to Mickstoy


